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Statoil’s investigation of Gudrun leak completed

May 20, 2015 14:10 CEST | Last modified September 12, 2019 10:25 CEST
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The Gudrun platform in the North Sea. (Photo: Eli Skjæveland Tengesdal)

In the morning of 18 February 2015 noise and vibrations were reported on Gudrun. Shortly afterwards hydrocarbons were confirmed in the process module.

There was a 2 mm wide crack extending approximately 90% across the circumference of a two-inch pipeline. Condensate had leaked from the pipeline and resulted in gas distribution. The actual leak rate is calculated to be around 8 kilogram/second.

The volume of condensate from the leak is estimated to 4 cubic metres.

No one was physically injured as no personnel were present in the area. The investigation concludes that the outcome could have been fatal if anybody had been exposed to the leak. A gas leak of this size represents a major incident potential if ignited.

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Øystein Arvid Håland, senior vice president of safety and sustainability of Development and Production Norway. (Photo: Harald Pettersen)

“The condensate leak on Gudrun was serious with major incident potential,” says Øystein Arvid Håland, senior vice president of safety and sustainability of Development and Production Norway.

“Statoil is working systematically on gas leak prevention, and the learnings from this incident shall be translated into specific actions. We must ensure that these efforts help prevent future incidents.”

Level valve

Based on material technical investigations the crack was the result of fatigue and overload. An under-dimensioned level valve led to vibrations in the valve itself and in the surrounding piping system during regular plant operation.

The vibrations resulted in loss of level valve control. The loss of valve control caused repeating powerful vibrations and strokes in the piping system which exceeded the design capacity.

No material defects, metallurgical irregularities or welding defects have been proven. The investigation team believes that pure chance prevented a full pipeline break.

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Bente Aleksandersen, senior vice president of the operations south cluster of Development and Production Norway. (Photo: Ivar Langvik)

The gas detectors recorded the leak, ignition sources were disconnected and the deluge system started automatically, as did the pressure relief system and the emergency shutdown system.

“I am glad that no one was physically injured,” says Bente Aleksandersen, senior vice president of the operations south cluster of Development and Production Norway.

“The investigation gives us valuable information to learn from and it is our responsibility to use this information both in Statoil and towards the Petroleum Safety Authority Norway (PSAN) and other players in the industry to prevent a recurrence of this type of incident. When the leak occurred, the emergency response system functioned as intended.”